並列タイトル等A Study of Air Breathing Rockets(III)-Supersonic Mode Combustors-
タイトル(掲載誌)航空宇宙技術研究所報告 = Technical Report of National Aerospace Laboratory TR-756
一般注記An experimental study was made on supersonic mode combustors of an air breathing rocket engine. Supersonic streams of room-temperature air and hot fuel-rich rocket exhaust were coaxially mixed and burned in a conically diverging duct of 2deg half-angle. The effect of air inlet Mach number and excess air ratio was investigated. Axial wall pressure distribution was measured to calculate one dimensional change of Mach number and stagnation temperature. Calculated results showed that supersonic combustion occurred in the duct. At the exit of the duct, gas sampling and Pitot pressure measurement was made, from which radial distributions of various properties were deduced. The distribution of mass fraction of elements from rocket exhaust showed poor mixing performance in the supersonic mode combustors compared with the previously investigated cylindrical subsonic mode combustors. Secondary combustion efficiency correlated well with the centerline mixing parameter, but not with Annushkin’s non-dimensional combustor length. No major effect of air inlet Mach number or excess air ratio was seen within the range of conditions under which the experiment was conducted.
資料番号: NALTR0756000
レポート番号: NAL TR-756
一次資料へのリンクURLhttps://jaxa.repo.nii.ac.jp/?action=repository_action_common_download&item_id=45014&item_no=1&attribute_id=31&file_no=1
連携機関・データベース国立情報学研究所 : 学術機関リポジトリデータベース(IRDB)(機関リポジトリ)
提供元機関・データベース宇宙航空研究開発機構 : 宇宙航空研究開発機構リポジトリ